Friday, July 1, 2011

And so it begins

New Website

Please check out my new website woodworkerb.com

Now it gets ugly.  Pulled the carbs, smog equipment, intake manifolds, exhaust header.  Every bolt and nut came out too nicely.  Until the last two.  One was stuck - could move back-and-forth a bit with vice-grips, the other stud (behind / below distributor) was already broken off.  At my neighbors urging, I elected to go with Metal Disintegrator Machining (MDM) through Jerry's Broken Drill and Tap Removal in Santa Ana California.  Glad I did - turns out someone already broke an EZ-Out in the other broken stud.  Both studs were removed and threaded inserts were placed.  $140 more to the tab, but beautiful results with zero damage to the head.

While it was out, I brought the head to Bob McKray Performance for cleaning and inspection.  Head was in excellent shape.  Manifold/header mounting area was .008" out-of-flat which was machined flat.  Valve seats re-ground.  Sandblasted clean - it is a thing of beauty.

Cylinder Head Before-and-After
Cylinder 1
Before-and-After

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